| Since then, I hooked up with Big
Steve.
We went to a swap meet put on by the
Antique Outboard Motor club and met this guy
who specialized in working on old
gas tanks and mid-century Johnson and Evinrude
motors. A couple of days later I took the Fish up to Sagamore
Hills (20 Mi. away) and Big Steve's house. Don, the earlier
mechanic, told me a number of things that needed to be fixed or replaced
and that he'd be glad to do it for $600.
Steve charged me half as much to make new gaskets
and diaphragm for the tank, re-build the carburetor, and get it running
much better. After a local test, Dale and I took the boats out to
West Branch State Park and ran for about an hour. The popping out
of gear problem persisted but was less of an issue because I could run
at higher speeds and it would pop out and in to gear occasionally. Just
as we decided to haul the boats out, the Fish died and I couldn't get it
restarted. Dale pulled me to shore with his boat.
I contacted Steve and hauled the boat back up to
Sagamore Hills. It seems that when he replaced baskets on the gas
tank, he didn't make a new seal for the gas cap and it leaked. He
made a new gasket for the gas cap, replaced the "clutch dog" (a little
gear looking thing at the top of the driveshaft), and a number of seals.
The motor started with a single pull of the rope. I've replaced
the starter and starter solenoid but haven't connected them yet.
The Fish seems to be running fine now. We
took the boats out to Portage Lakes last Sunday and putted around for a
couple of hours. We even stopped at a couple of the lakeside bars
and had a cold one. The Fish started right up and ran without
jumping out of gear. Dale took a short video with his still
camera. The link to the video is on the left. |